Back analysis and rectification of a failed cut slope in the Southern Expressway

dc.contributor.authorDharmasena, UKNP
dc.contributor.authorBandara, KN
dc.contributor.authorKarunawardena, WA
dc.contributor.authorKulathilaka, SAS
dc.date.accessioned2017-11-23T15:35:17Z
dc.date.available2017-11-23T15:35:17Z
dc.description.abstractA failure occurred in a cut slope of the southern expressway where all the surface drainage measures had been implemented. The failure surface was shallow but it has disrupted three levels of berms. The debris of failure were quite dry. A close examination indicated that a cascade drain has cracked and water is leaking to the slope. There were five systems of joints in the rock and adversely oriented relict joints were identified during rectification work . The failure could have been triggered by infiltration of rainwater through relict joints , reduction of matric suction and development of pore pressure . Rectification process involved installation of soil nailing and cable anchoring together with long sub horizontal drains.en_US
dc.identifier.conferenceInternational Conference on Geotechnical Engineering - (ICGE) 2015en_US
dc.identifier.departmentDepartment of Civil Engineeringen_US
dc.identifier.facultyEngineeringen_US
dc.identifier.pgnospp. 543 546en_US
dc.identifier.placeColomboen_US
dc.identifier.urihttp://dl.lib.mrt.ac.lk/handle/123/12898
dc.identifier.year2015en_US
dc.language.isoenen_US
dc.titleBack analysis and rectification of a failed cut slope in the Southern Expresswayen_US
dc.typeConference-Abstracten_US

Files